1980 CB750K Carb Issues
Posted by rhinocb750k on May 28, 2013; 5:03pm
URL: http://vintage-and-classic-hondas.81.s1.nabble.com/1980-CB750K-Carb-Issues-tp4041372.html
Hi guys, looking for some help.
I have had my bike for a couple years with no issues. My problem started with a needle valve issue with fuel coming out of the overflow. I decided at that point to do a cleaning of all 4 carbs (bank assembled) and new needle valves. After cleaning I decided to include the air cut bypass during assembly. I backed out the pilot needle 3-1/2 turns. Bike Runs but is lean at idle even after warm up. I checked for leaks at the intake boots but found none. At this point i figured there must be something clogged in the fixed idle jet. Removed the carbs again and cleaned them again and made sure I could run a wire down the fixed passage and blow cleaner through the circuit. I reinstalled them and had the same problem. Bike is lean. No matter how much I back out the pilot needle it is lean. Any ideas to my problem. The only thing I changed is the air cut bypass. Should I not bypass the air cut? Anyone else had this problem? Any help would be appreciated. Thanks
-stock jets 68 primary, 102 secondary
-stock air box/filter
-exhaust is stock 4x4 but previous owner cut most of the mufflers off